#21
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2. Installed one last time. 3. View from the top. You might notice that I turned the bearing sleeve upside down from the first time I showed it because the bearing is now flush on top. It just worked out better that way for installing the brace. For some reason I left about 3/8ths" of the other sleeve extending out downwards & exposed. I either forgot to trim it or or just decided I didn't care. As my dad used to say, "It ain't hurtin' anything" so I probably decided just that. Mildred doesn't care either. 4. We had a visitor at some point; I believe it was in November of 2014. I can tell from this picture that I was still tinkering with it because the lower socket is still clamped to the base in this picture. This picture shows you a pretty good view of the overall thing from the front side. 5. I did eventually screw the last part down after I was through tweaking it as best I could. I actually wound up forcing the socket forward a little bit to sort of preload a little bit of pressure on the guide rod. Only then did I locate and drill & tap the final two hole in the base. It just worked better that way. That few pounds of force on the guide rod was the key for getting the loss of registration down from .0010" or .0015" to the .0001" -.0004" that it is now. Now a final word or several about that reading: The test bar that I was using is hardly guaranteed straight anyway. It is a possibly 75 year old boring bar from my maternal grandfather's machinist chest. Secondly, the spindle and the quill don't necessarily run absolutely true either, neither up & down or in rotation. There can easily be a thousandth or two runout using any tool you stick in the collet. This was after all, a $400 Harbor Freight mill to begin with.
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cutter Housekeeping Staff: the Gatekeeper Director of Policy, Syntax and Grammar (by appointment) "Dr. Chandran, will I dream?" Just Keep Walking "I am not a body, I am free. For I am still as God created me." |
#22
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Quote:
The only conclusion I can reach is that your mill must not, indeed cannot, have as much inherent tendency to twist built into it to as Mildred does. I have no way of measuring the amount of force involved but it is surprising. There really is no reason to expect that two Rong Fu mills from even the same production run would behave the same way anyhow. If Miner did want to rotate as badly as Mildred then I believe it would shift something in your yokes or in the crank assembly, or I bet you that 3/4" bar would flex enough under travel to be very noticeable. She definitely flexed the 3/4" bar I used on my first attempt. That's one reason I bolted and braced the lower mount to Mildred's base instead of using a second yoke. I also figured the 1 inch bar was too heavy to be supported by the yoke arrangement. Clive, I found one more picture of the overall assembly from the backside.
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cutter Housekeeping Staff: the Gatekeeper Director of Policy, Syntax and Grammar (by appointment) "Dr. Chandran, will I dream?" Just Keep Walking "I am not a body, I am free. For I am still as God created me." |
#23
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Very nice job!!!! with a lot of head scratchen I bet. Any idea about time it would take to do another verses the time that you have in this build
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Drawing by Smartdraw |
#24
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After looking at the back side of your bar/mounts, I can see where it should work similar to Miner's.
Maybe the torque of the motor is trying to twist the head?
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Mark I haven't always been a nurse.......... Oxy/Acetylene set Hand/Power tools Harbor Freight Tubing Roller Craftsman 12 x 36 lathe New to me Enco GL-30B Mill/Drill Thank you 1800Miner Papa Lion's Gate Build I don't do nuttin half azzed. I phawk it up completely, given half a chance. |
#25
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Nope.
In the first place I've watched it go up & down at least a hundred times, more actually, without the guide bar. It will wave back & forth past center some of the time & does not necessarily ever behave exactly the same way two times in a row. It does favor moving to the left more than to the right. Secondly, the motor is mounted to the head casting so any "torque" would be like an isometric exercise, pulling against itself. As far as drive motor rotational or centrifugal torque, it is horizontal, 90° to the column. Third, the dc motor is variable speed, meaning that I can soft start it but no matter whether I ease into it or start it fast the head will move at some point during travel, not necessarily at the beginning. And it always liked to move more towards the top of the travel. It always moved radically when I had to crank it. Quote:
Then there are parts. I only had the one 1 inch bar. The only parts I had to buy was a 1" bushing 6 inches long but I would have to find/buy another chrome rod. Duplicating the yoke & the base plates would be easy and I would definitely want to simplify the bearing carrier sleeve situation. No way I want to bore out another chunk of that 2 inch bar, which was probably an axle but whatever it was, it was something extremely tedious for me to work. So right away I'd get into changing the plan. If I could find a 2 inch slug already drilled out to 1 inch it would certainly simply that. There still has to be some way to align the bearings perfectly in line with the column. I believe that it has to turn out with less than one degree or error. I wouldn't expect anyone else to approach it the way I did. On the other hand, it did work. But there should be an easier way. The real nut is I wouldn't have high expectation of this working without getting rid of that crank. I think the dc motor drive makes it possible by turning the gear without a bunch of jerking back & forth. That part of the project - building the power lift - took a lot of time too. I don't have another 1/4 hp dc gearmotor like that either. So the answer is, I really don't know but I am definitely glad I don't have to do it again.
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cutter Housekeeping Staff: the Gatekeeper Director of Policy, Syntax and Grammar (by appointment) "Dr. Chandran, will I dream?" Just Keep Walking "I am not a body, I am free. For I am still as God created me." |
#26
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I really like the dc motor lift, I will let it simmer away for a while before I start but I will definately motorise the lift. Many thanks for all the photos.
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It's So Easy |
#27
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Quote:
As usual, this was an experimental prototype, wordy & tedious build project with lots of sidetracking & me just having fun. But I did learn a few things along the way so it might be helpful to you if you haven't read it. Reading it again highlighted the importance of one thing: if you use new sprockets, which I did, use new chain! It will probably save you a lot of screwing around. I happened to have a bucket full of used #50 roller chain that Old Man sent me several years ago for some reason & I tried using it just because I had it. Caused me a lot of lost time until Ironman pointed out the folly. I can assure you this is worth doing for anyone who has one of these little mill/drills. I was very negligent about moving the head to facilitate tool or collet/chuck changes so long as I had to crank the thing up & down. This meant I would likely try to run Mildred with the head too far away from the work, spindle extended, a lot of the time so I could switch between collets & drill chucks without moving the head. Or I would shift the work between the mill & the drill press instead of using Mildred for both operations just to avoid that damned uncomfortable crank.
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cutter Housekeeping Staff: the Gatekeeper Director of Policy, Syntax and Grammar (by appointment) "Dr. Chandran, will I dream?" Just Keep Walking "I am not a body, I am free. For I am still as God created me." |
#28
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I read through this whole thread again and think it's worth trying, maybe this winter.
A video popped up yesterday, of a fellow in Australia named Bruce Whitham, who is manufacturing a kit called the, "Line 8." He has come up with a way to stabilize the head, while retaining the ability to swivel the head and then, re-lock it. Unfortunately, to buy it and get it shipped to the U.S. would be at least $500.00 That's all I paid for the whole machine. I began trying to source the material to try and duplicate it but, the Delrin he uses for his bearing material is outrageously expensive because, so far, I've only been able to find a piece 12"x12"x4" thick. The cost would be over $250.00. That's six times the amount of material needed, to boot. Time to do a little "noodlin' " of my own. Dave
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Hoocha Momma!, who chop-id-da cheese? |
#29
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Quote:
If I had a need to swivel it then I would have somehow designed the interface between the bearing and Mildred's head to disconnect. I could do that now but it would not maintain registration in any other position.
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cutter Housekeeping Staff: the Gatekeeper Director of Policy, Syntax and Grammar (by appointment) "Dr. Chandran, will I dream?" Just Keep Walking "I am not a body, I am free. For I am still as God created me." |
#30
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Just looked at this thread: What happened to Mark Ball ??? I noticed he had a post or so on this.
...lew... |
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